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#81
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HELP! Hafler DH-200 misbehaving!
"John A. Weeks III" wrote: In article , Dick West wrote: I would first check those 4 transistors. Remember, they must be used in pairs matched for hFe, else DC offset results. Did the original poster ever remove the MOSFET's from the unit. If so, were they put back in exactly the same place? If not, it is possible that the matched sets were mismatched in the process. That would be enough to cause the problem that Dick is talking about. -john- John, if I recall parts of this thread correctly, the OP said that he also found one of the DC power supply wires to the circuit card was not attached. Obviously, this would cause a huge set of problems such as he described. Now, we do know that the two N-channel MOSFETs on a channel must be matched on Vge within 10%, which is why each MOSFET is marked with the Hafler grading number. Ditto for the P-channel MOSFETs. These devices are not the same 4 to which I referred. I referred to the 4 input differential amp circuit on the circuit card which must be matched, not the 4 MOSFETs attached to the heatsink. Let's wait to hear more from the OP before making anymore guesses about what is wrong. Besides, without the use of a Variac his efforts are probably doomed to failure. Dick |
#82
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HELP! Hafler DH-200 misbehaving!
John A. Weeks III wrote:
Did the original poster ever remove the MOSFET's from the unit. If so, were they put back in exactly the same place? If not, it is possible that the matched sets were mismatched in the process. That would be enough to cause the problem that Dick is talking about. Here I am, the original poster! :-) I removed the MOSFETS at one point, and they all went back into the same slots. Exactly. And as for Dick's suggestions, let me recap and intersperse a few questions. 1) Q9, the transistor in the bias circuit, was definitely fried. It was measuring a hfE between 200 and 1700, depending on the time of day, when we tested it out of circuit. (specs for it should be about 60). And yes, the reading changed drastically from hour to hour. 2) Replacing it and fixing a broken solder joint seemed to fix things, but after something less than three hours of playing, it died again. This time the speaker fuse was shot as well, and when I replaced it, I was back to the same scenario I had before replacing Q9. The symptoms a -20VDC at the speaker outputs. No sound to the speaker. (But I'm not about to hook them up again!) 3) And for the record, for that brief while that the amp was working, the DC output at the speaker terminals was tiny--definitely less than 80mV. (with no input signal, of course) So my plan is to check Q9 again, and I'm expecting to find it dead. After that, I'll go after the Q1/Q2 pair, and see if they've drifted apart. Next will be the opposite pair, Q5 and Q6 I believe (I don't have the schematic in front of me). After that, it's going to be a process of testing every resistor, diode, and cap on the board. Then--MAYBE--I'll plug it in again. Colin |
#83
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HELP! Hafler DH-200 misbehaving!
John A. Weeks III wrote:
Did the original poster ever remove the MOSFET's from the unit. If so, were they put back in exactly the same place? If not, it is possible that the matched sets were mismatched in the process. That would be enough to cause the problem that Dick is talking about. Here I am, the original poster! :-) I removed the MOSFETS at one point, and they all went back into the same slots. Exactly. And as for Dick's suggestions, let me recap and intersperse a few questions. 1) Q9, the transistor in the bias circuit, was definitely fried. It was measuring a hfE between 200 and 1700, depending on the time of day, when we tested it out of circuit. (specs for it should be about 60). And yes, the reading changed drastically from hour to hour. 2) Replacing it and fixing a broken solder joint seemed to fix things, but after something less than three hours of playing, it died again. This time the speaker fuse was shot as well, and when I replaced it, I was back to the same scenario I had before replacing Q9. The symptoms a -20VDC at the speaker outputs. No sound to the speaker. (But I'm not about to hook them up again!) 3) And for the record, for that brief while that the amp was working, the DC output at the speaker terminals was tiny--definitely less than 80mV. (with no input signal, of course) So my plan is to check Q9 again, and I'm expecting to find it dead. After that, I'll go after the Q1/Q2 pair, and see if they've drifted apart. Next will be the opposite pair, Q5 and Q6 I believe (I don't have the schematic in front of me). After that, it's going to be a process of testing every resistor, diode, and cap on the board. Then--MAYBE--I'll plug it in again. Colin |
#84
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HELP! Hafler DH-200 misbehaving!
John A. Weeks III wrote:
Did the original poster ever remove the MOSFET's from the unit. If so, were they put back in exactly the same place? If not, it is possible that the matched sets were mismatched in the process. That would be enough to cause the problem that Dick is talking about. Here I am, the original poster! :-) I removed the MOSFETS at one point, and they all went back into the same slots. Exactly. And as for Dick's suggestions, let me recap and intersperse a few questions. 1) Q9, the transistor in the bias circuit, was definitely fried. It was measuring a hfE between 200 and 1700, depending on the time of day, when we tested it out of circuit. (specs for it should be about 60). And yes, the reading changed drastically from hour to hour. 2) Replacing it and fixing a broken solder joint seemed to fix things, but after something less than three hours of playing, it died again. This time the speaker fuse was shot as well, and when I replaced it, I was back to the same scenario I had before replacing Q9. The symptoms a -20VDC at the speaker outputs. No sound to the speaker. (But I'm not about to hook them up again!) 3) And for the record, for that brief while that the amp was working, the DC output at the speaker terminals was tiny--definitely less than 80mV. (with no input signal, of course) So my plan is to check Q9 again, and I'm expecting to find it dead. After that, I'll go after the Q1/Q2 pair, and see if they've drifted apart. Next will be the opposite pair, Q5 and Q6 I believe (I don't have the schematic in front of me). After that, it's going to be a process of testing every resistor, diode, and cap on the board. Then--MAYBE--I'll plug it in again. Colin |
#85
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HELP! Hafler DH-200 misbehaving!
John A. Weeks III wrote:
Did the original poster ever remove the MOSFET's from the unit. If so, were they put back in exactly the same place? If not, it is possible that the matched sets were mismatched in the process. That would be enough to cause the problem that Dick is talking about. Here I am, the original poster! :-) I removed the MOSFETS at one point, and they all went back into the same slots. Exactly. And as for Dick's suggestions, let me recap and intersperse a few questions. 1) Q9, the transistor in the bias circuit, was definitely fried. It was measuring a hfE between 200 and 1700, depending on the time of day, when we tested it out of circuit. (specs for it should be about 60). And yes, the reading changed drastically from hour to hour. 2) Replacing it and fixing a broken solder joint seemed to fix things, but after something less than three hours of playing, it died again. This time the speaker fuse was shot as well, and when I replaced it, I was back to the same scenario I had before replacing Q9. The symptoms a -20VDC at the speaker outputs. No sound to the speaker. (But I'm not about to hook them up again!) 3) And for the record, for that brief while that the amp was working, the DC output at the speaker terminals was tiny--definitely less than 80mV. (with no input signal, of course) So my plan is to check Q9 again, and I'm expecting to find it dead. After that, I'll go after the Q1/Q2 pair, and see if they've drifted apart. Next will be the opposite pair, Q5 and Q6 I believe (I don't have the schematic in front of me). After that, it's going to be a process of testing every resistor, diode, and cap on the board. Then--MAYBE--I'll plug it in again. Colin |
#86
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HELP! Hafler DH-200 misbehaving!
"Colin B." wrote:
John A. Weeks III wrote: Did the original poster ever remove the MOSFET's from the unit. If so, were they put back in exactly the same place? If not, it is possible that the matched sets were mismatched in the process. That would be enough to cause the problem that Dick is talking about. Here I am, the original poster! :-) I removed the MOSFETS at one point, and they all went back into the same slots. Exactly. And as for Dick's suggestions, let me recap and intersperse a few questions. 1) Q9, the transistor in the bias circuit, was definitely fried. It was measuring a hfE between 200 and 1700, depending on the time of day, when we tested it out of circuit. (specs for it should be about 60). And yes, the reading changed drastically from hour to hour. 2) Replacing it and fixing a broken solder joint seemed to fix things, but after something less than three hours of playing, it died again. This time the speaker fuse was shot as well, and when I replaced it, I was back to the same scenario I had before replacing Q9. The symptoms a -20VDC at the speaker outputs. No sound to the speaker. (But I'm not about to hook them up again!) 3) And for the record, for that brief while that the amp was working, the DC output at the speaker terminals was tiny--definitely less than 80mV. (with no input signal, of course) So my plan is to check Q9 again, and I'm expecting to find it dead. After that, I'll go after the Q1/Q2 pair, and see if they've drifted apart. Next will be the opposite pair, Q5 and Q6 I believe (I don't have the schematic in front of me). After that, it's going to be a process of testing every resistor, diode, and cap on the board. Then--MAYBE--I'll plug it in again. Colin Colin, this is Dick, the "HaflerLover." Thanks for summarizing your progress. Here are some suggestions and opinions: 1. I doubt Q9 is the main offender. Its hfe should be around 150 but a modestly lower or higher hfe will result mostly in the inability of P1 to adjust the amount of bias current. You seem to be getting dramatic changes in voltages as a function of time (and probably temperature) too large to be related just to bias adjustment. 2. Dramatic changes in parameters that seem related to temperature could be caused by a break (a lesion) in a trace, a solder joint, or even an internal connection in an active device (transistor or diode) or a resistor. Things expand and contract due to temperature and only a microscopic circuit break is required to produce significant changes in output. But, without better control in input AC voltage it is difficult to track down this type of problem. You need a Variac. However a change in DC offset from 80 mV to 20V is dramatic and makes me think you have an either/or thing going on, such as a temperature related break in the circuit or a component. Here is a repair strategy to consider: 1. Get a Variac or wire up 2-3 60 watt light bulbs in series with the input AC. By switching a bypass to each bulb in turn you can slowly ramp up the input AC surge and voltage -- giving you some control over events in the circuit. 2. Use two meters, a Variac, a can of "cool-it" and a heat gun (hair dryer). Monitor bias current and DC offset voltage with the two meters as you slowly ramp up the incoming AC voltage. Put a 10 ohm 10 watt resistor across the speaker outputs in the channel under test. This will help you more reliably test for DC offset when you connect meter probes. And, make all voltage measurements related to circuit ground -- the connection between the two power supply filter caps. Selectively heat and cool various transistors and monitor the effect of these events by watching the changes in bias and, especially, the DC offset. This will help you make some assumptions about which part of the circuit is bad. Also, use a plastic tool (toothbrush handle) to tap or gently strike various components and circuit traces to see if doing so changes the readings on the meters. This process may help you find any small circuit breaks that might exist. On one occasion I took the time to reflow all solder joints on the back of one circuit card that was causing a problem, and doing this fixed the circuit. 3. What color is your circuit card? Is it phenolic board or the gray-green fiberglass? What is the serial number of your amp? It is on a 2" square white sticker on the bottom or back side of your amp. There were 3 revisions to the DH-200 and I can tell you which you have based on the serial number. Earlier amps with phenolic cards often had microscopic dry solder joints around the driver and pre-driver transistors (the 4 with the cooling fins). This was because the solder bath temp and time this card could tolerate was too low to produce good joints all of the time. Later versions of the amp used a small plastic washer at the bottom of each of these 4 transistors and the attachment of the traces on the rear of the card was improved (better glue), which resulted in higher tolerances in solder bath time and temperatures which resulted in improved solder connections without heat damage to components. As a minimum I would re-flow the solder joints around the BCE of these four transistors, the ones with the small metal can tops. 4. And, of course, you should check for the obvious. Broken wires or bad solder joints in other parts of the amp, especially power supply connections and the feedback to the amp from the speaker protection fuse. However because your problem is only with one channel I doubt anything is wrong with the power supply unless it is a power supply connection to the card. You could monitor the voltages at the + and - supply rails on the card as you tap its components and its connections back to the PS. They should be ~65 +/- VDC. 5. You should lay out both heat sinks to enable access to both circuit cards. Then compare voltages at suspicious parts by noting voltages on the good circuit and the same spot on the bad card. But, of course, this prolonged comparison of voltages works best when a variac is used so you can keep the bad card at energized at a low voltage that precludes blowing up or frying the rest of its channel. Well, that's enough for now and I am sure enough to draw some flames from others. Tell me the serial number and I will make other suggestions. Dick |
#87
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HELP! Hafler DH-200 misbehaving!
"Colin B." wrote:
John A. Weeks III wrote: Did the original poster ever remove the MOSFET's from the unit. If so, were they put back in exactly the same place? If not, it is possible that the matched sets were mismatched in the process. That would be enough to cause the problem that Dick is talking about. Here I am, the original poster! :-) I removed the MOSFETS at one point, and they all went back into the same slots. Exactly. And as for Dick's suggestions, let me recap and intersperse a few questions. 1) Q9, the transistor in the bias circuit, was definitely fried. It was measuring a hfE between 200 and 1700, depending on the time of day, when we tested it out of circuit. (specs for it should be about 60). And yes, the reading changed drastically from hour to hour. 2) Replacing it and fixing a broken solder joint seemed to fix things, but after something less than three hours of playing, it died again. This time the speaker fuse was shot as well, and when I replaced it, I was back to the same scenario I had before replacing Q9. The symptoms a -20VDC at the speaker outputs. No sound to the speaker. (But I'm not about to hook them up again!) 3) And for the record, for that brief while that the amp was working, the DC output at the speaker terminals was tiny--definitely less than 80mV. (with no input signal, of course) So my plan is to check Q9 again, and I'm expecting to find it dead. After that, I'll go after the Q1/Q2 pair, and see if they've drifted apart. Next will be the opposite pair, Q5 and Q6 I believe (I don't have the schematic in front of me). After that, it's going to be a process of testing every resistor, diode, and cap on the board. Then--MAYBE--I'll plug it in again. Colin Colin, this is Dick, the "HaflerLover." Thanks for summarizing your progress. Here are some suggestions and opinions: 1. I doubt Q9 is the main offender. Its hfe should be around 150 but a modestly lower or higher hfe will result mostly in the inability of P1 to adjust the amount of bias current. You seem to be getting dramatic changes in voltages as a function of time (and probably temperature) too large to be related just to bias adjustment. 2. Dramatic changes in parameters that seem related to temperature could be caused by a break (a lesion) in a trace, a solder joint, or even an internal connection in an active device (transistor or diode) or a resistor. Things expand and contract due to temperature and only a microscopic circuit break is required to produce significant changes in output. But, without better control in input AC voltage it is difficult to track down this type of problem. You need a Variac. However a change in DC offset from 80 mV to 20V is dramatic and makes me think you have an either/or thing going on, such as a temperature related break in the circuit or a component. Here is a repair strategy to consider: 1. Get a Variac or wire up 2-3 60 watt light bulbs in series with the input AC. By switching a bypass to each bulb in turn you can slowly ramp up the input AC surge and voltage -- giving you some control over events in the circuit. 2. Use two meters, a Variac, a can of "cool-it" and a heat gun (hair dryer). Monitor bias current and DC offset voltage with the two meters as you slowly ramp up the incoming AC voltage. Put a 10 ohm 10 watt resistor across the speaker outputs in the channel under test. This will help you more reliably test for DC offset when you connect meter probes. And, make all voltage measurements related to circuit ground -- the connection between the two power supply filter caps. Selectively heat and cool various transistors and monitor the effect of these events by watching the changes in bias and, especially, the DC offset. This will help you make some assumptions about which part of the circuit is bad. Also, use a plastic tool (toothbrush handle) to tap or gently strike various components and circuit traces to see if doing so changes the readings on the meters. This process may help you find any small circuit breaks that might exist. On one occasion I took the time to reflow all solder joints on the back of one circuit card that was causing a problem, and doing this fixed the circuit. 3. What color is your circuit card? Is it phenolic board or the gray-green fiberglass? What is the serial number of your amp? It is on a 2" square white sticker on the bottom or back side of your amp. There were 3 revisions to the DH-200 and I can tell you which you have based on the serial number. Earlier amps with phenolic cards often had microscopic dry solder joints around the driver and pre-driver transistors (the 4 with the cooling fins). This was because the solder bath temp and time this card could tolerate was too low to produce good joints all of the time. Later versions of the amp used a small plastic washer at the bottom of each of these 4 transistors and the attachment of the traces on the rear of the card was improved (better glue), which resulted in higher tolerances in solder bath time and temperatures which resulted in improved solder connections without heat damage to components. As a minimum I would re-flow the solder joints around the BCE of these four transistors, the ones with the small metal can tops. 4. And, of course, you should check for the obvious. Broken wires or bad solder joints in other parts of the amp, especially power supply connections and the feedback to the amp from the speaker protection fuse. However because your problem is only with one channel I doubt anything is wrong with the power supply unless it is a power supply connection to the card. You could monitor the voltages at the + and - supply rails on the card as you tap its components and its connections back to the PS. They should be ~65 +/- VDC. 5. You should lay out both heat sinks to enable access to both circuit cards. Then compare voltages at suspicious parts by noting voltages on the good circuit and the same spot on the bad card. But, of course, this prolonged comparison of voltages works best when a variac is used so you can keep the bad card at energized at a low voltage that precludes blowing up or frying the rest of its channel. Well, that's enough for now and I am sure enough to draw some flames from others. Tell me the serial number and I will make other suggestions. Dick |
#88
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HELP! Hafler DH-200 misbehaving!
"Colin B." wrote:
John A. Weeks III wrote: Did the original poster ever remove the MOSFET's from the unit. If so, were they put back in exactly the same place? If not, it is possible that the matched sets were mismatched in the process. That would be enough to cause the problem that Dick is talking about. Here I am, the original poster! :-) I removed the MOSFETS at one point, and they all went back into the same slots. Exactly. And as for Dick's suggestions, let me recap and intersperse a few questions. 1) Q9, the transistor in the bias circuit, was definitely fried. It was measuring a hfE between 200 and 1700, depending on the time of day, when we tested it out of circuit. (specs for it should be about 60). And yes, the reading changed drastically from hour to hour. 2) Replacing it and fixing a broken solder joint seemed to fix things, but after something less than three hours of playing, it died again. This time the speaker fuse was shot as well, and when I replaced it, I was back to the same scenario I had before replacing Q9. The symptoms a -20VDC at the speaker outputs. No sound to the speaker. (But I'm not about to hook them up again!) 3) And for the record, for that brief while that the amp was working, the DC output at the speaker terminals was tiny--definitely less than 80mV. (with no input signal, of course) So my plan is to check Q9 again, and I'm expecting to find it dead. After that, I'll go after the Q1/Q2 pair, and see if they've drifted apart. Next will be the opposite pair, Q5 and Q6 I believe (I don't have the schematic in front of me). After that, it's going to be a process of testing every resistor, diode, and cap on the board. Then--MAYBE--I'll plug it in again. Colin Colin, this is Dick, the "HaflerLover." Thanks for summarizing your progress. Here are some suggestions and opinions: 1. I doubt Q9 is the main offender. Its hfe should be around 150 but a modestly lower or higher hfe will result mostly in the inability of P1 to adjust the amount of bias current. You seem to be getting dramatic changes in voltages as a function of time (and probably temperature) too large to be related just to bias adjustment. 2. Dramatic changes in parameters that seem related to temperature could be caused by a break (a lesion) in a trace, a solder joint, or even an internal connection in an active device (transistor or diode) or a resistor. Things expand and contract due to temperature and only a microscopic circuit break is required to produce significant changes in output. But, without better control in input AC voltage it is difficult to track down this type of problem. You need a Variac. However a change in DC offset from 80 mV to 20V is dramatic and makes me think you have an either/or thing going on, such as a temperature related break in the circuit or a component. Here is a repair strategy to consider: 1. Get a Variac or wire up 2-3 60 watt light bulbs in series with the input AC. By switching a bypass to each bulb in turn you can slowly ramp up the input AC surge and voltage -- giving you some control over events in the circuit. 2. Use two meters, a Variac, a can of "cool-it" and a heat gun (hair dryer). Monitor bias current and DC offset voltage with the two meters as you slowly ramp up the incoming AC voltage. Put a 10 ohm 10 watt resistor across the speaker outputs in the channel under test. This will help you more reliably test for DC offset when you connect meter probes. And, make all voltage measurements related to circuit ground -- the connection between the two power supply filter caps. Selectively heat and cool various transistors and monitor the effect of these events by watching the changes in bias and, especially, the DC offset. This will help you make some assumptions about which part of the circuit is bad. Also, use a plastic tool (toothbrush handle) to tap or gently strike various components and circuit traces to see if doing so changes the readings on the meters. This process may help you find any small circuit breaks that might exist. On one occasion I took the time to reflow all solder joints on the back of one circuit card that was causing a problem, and doing this fixed the circuit. 3. What color is your circuit card? Is it phenolic board or the gray-green fiberglass? What is the serial number of your amp? It is on a 2" square white sticker on the bottom or back side of your amp. There were 3 revisions to the DH-200 and I can tell you which you have based on the serial number. Earlier amps with phenolic cards often had microscopic dry solder joints around the driver and pre-driver transistors (the 4 with the cooling fins). This was because the solder bath temp and time this card could tolerate was too low to produce good joints all of the time. Later versions of the amp used a small plastic washer at the bottom of each of these 4 transistors and the attachment of the traces on the rear of the card was improved (better glue), which resulted in higher tolerances in solder bath time and temperatures which resulted in improved solder connections without heat damage to components. As a minimum I would re-flow the solder joints around the BCE of these four transistors, the ones with the small metal can tops. 4. And, of course, you should check for the obvious. Broken wires or bad solder joints in other parts of the amp, especially power supply connections and the feedback to the amp from the speaker protection fuse. However because your problem is only with one channel I doubt anything is wrong with the power supply unless it is a power supply connection to the card. You could monitor the voltages at the + and - supply rails on the card as you tap its components and its connections back to the PS. They should be ~65 +/- VDC. 5. You should lay out both heat sinks to enable access to both circuit cards. Then compare voltages at suspicious parts by noting voltages on the good circuit and the same spot on the bad card. But, of course, this prolonged comparison of voltages works best when a variac is used so you can keep the bad card at energized at a low voltage that precludes blowing up or frying the rest of its channel. Well, that's enough for now and I am sure enough to draw some flames from others. Tell me the serial number and I will make other suggestions. Dick |
#89
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HELP! Hafler DH-200 misbehaving!
"Colin B." wrote:
John A. Weeks III wrote: Did the original poster ever remove the MOSFET's from the unit. If so, were they put back in exactly the same place? If not, it is possible that the matched sets were mismatched in the process. That would be enough to cause the problem that Dick is talking about. Here I am, the original poster! :-) I removed the MOSFETS at one point, and they all went back into the same slots. Exactly. And as for Dick's suggestions, let me recap and intersperse a few questions. 1) Q9, the transistor in the bias circuit, was definitely fried. It was measuring a hfE between 200 and 1700, depending on the time of day, when we tested it out of circuit. (specs for it should be about 60). And yes, the reading changed drastically from hour to hour. 2) Replacing it and fixing a broken solder joint seemed to fix things, but after something less than three hours of playing, it died again. This time the speaker fuse was shot as well, and when I replaced it, I was back to the same scenario I had before replacing Q9. The symptoms a -20VDC at the speaker outputs. No sound to the speaker. (But I'm not about to hook them up again!) 3) And for the record, for that brief while that the amp was working, the DC output at the speaker terminals was tiny--definitely less than 80mV. (with no input signal, of course) So my plan is to check Q9 again, and I'm expecting to find it dead. After that, I'll go after the Q1/Q2 pair, and see if they've drifted apart. Next will be the opposite pair, Q5 and Q6 I believe (I don't have the schematic in front of me). After that, it's going to be a process of testing every resistor, diode, and cap on the board. Then--MAYBE--I'll plug it in again. Colin Colin, this is Dick, the "HaflerLover." Thanks for summarizing your progress. Here are some suggestions and opinions: 1. I doubt Q9 is the main offender. Its hfe should be around 150 but a modestly lower or higher hfe will result mostly in the inability of P1 to adjust the amount of bias current. You seem to be getting dramatic changes in voltages as a function of time (and probably temperature) too large to be related just to bias adjustment. 2. Dramatic changes in parameters that seem related to temperature could be caused by a break (a lesion) in a trace, a solder joint, or even an internal connection in an active device (transistor or diode) or a resistor. Things expand and contract due to temperature and only a microscopic circuit break is required to produce significant changes in output. But, without better control in input AC voltage it is difficult to track down this type of problem. You need a Variac. However a change in DC offset from 80 mV to 20V is dramatic and makes me think you have an either/or thing going on, such as a temperature related break in the circuit or a component. Here is a repair strategy to consider: 1. Get a Variac or wire up 2-3 60 watt light bulbs in series with the input AC. By switching a bypass to each bulb in turn you can slowly ramp up the input AC surge and voltage -- giving you some control over events in the circuit. 2. Use two meters, a Variac, a can of "cool-it" and a heat gun (hair dryer). Monitor bias current and DC offset voltage with the two meters as you slowly ramp up the incoming AC voltage. Put a 10 ohm 10 watt resistor across the speaker outputs in the channel under test. This will help you more reliably test for DC offset when you connect meter probes. And, make all voltage measurements related to circuit ground -- the connection between the two power supply filter caps. Selectively heat and cool various transistors and monitor the effect of these events by watching the changes in bias and, especially, the DC offset. This will help you make some assumptions about which part of the circuit is bad. Also, use a plastic tool (toothbrush handle) to tap or gently strike various components and circuit traces to see if doing so changes the readings on the meters. This process may help you find any small circuit breaks that might exist. On one occasion I took the time to reflow all solder joints on the back of one circuit card that was causing a problem, and doing this fixed the circuit. 3. What color is your circuit card? Is it phenolic board or the gray-green fiberglass? What is the serial number of your amp? It is on a 2" square white sticker on the bottom or back side of your amp. There were 3 revisions to the DH-200 and I can tell you which you have based on the serial number. Earlier amps with phenolic cards often had microscopic dry solder joints around the driver and pre-driver transistors (the 4 with the cooling fins). This was because the solder bath temp and time this card could tolerate was too low to produce good joints all of the time. Later versions of the amp used a small plastic washer at the bottom of each of these 4 transistors and the attachment of the traces on the rear of the card was improved (better glue), which resulted in higher tolerances in solder bath time and temperatures which resulted in improved solder connections without heat damage to components. As a minimum I would re-flow the solder joints around the BCE of these four transistors, the ones with the small metal can tops. 4. And, of course, you should check for the obvious. Broken wires or bad solder joints in other parts of the amp, especially power supply connections and the feedback to the amp from the speaker protection fuse. However because your problem is only with one channel I doubt anything is wrong with the power supply unless it is a power supply connection to the card. You could monitor the voltages at the + and - supply rails on the card as you tap its components and its connections back to the PS. They should be ~65 +/- VDC. 5. You should lay out both heat sinks to enable access to both circuit cards. Then compare voltages at suspicious parts by noting voltages on the good circuit and the same spot on the bad card. But, of course, this prolonged comparison of voltages works best when a variac is used so you can keep the bad card at energized at a low voltage that precludes blowing up or frying the rest of its channel. Well, that's enough for now and I am sure enough to draw some flames from others. Tell me the serial number and I will make other suggestions. Dick |
#91
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HELP! Hafler DH-200 misbehaving!
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#92
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HELP! Hafler DH-200 misbehaving!
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#93
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HELP! Hafler DH-200 misbehaving!
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#94
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HELP! Hafler DH-200 misbehaving!
In article ,
Colin B. wrote: Good point. I'm tempted to reflow the board as it is, just because. When we saw the one bad power lead on the board, we did touch up all of the connecting wires (none of them looked very good, actually) but not on the board itself. Speaking of which, it's a phenolic board on this amp. I don't have the serial number right now, but I'll get it when I go home. I'll look closely, but I don't think there are any washers between the transistors and the board, anywhere. I had (have) a Van Alstine Omega 150 amp which developed some odd symptoms - a sharp POP in one channel, anywhere from 15 seconds to a couple of minutes after it was powered on. This occurred intermittently for a couple of years, and then the channel suddenly became extremely noisy (hiss). I phoned AVA, and Frank Van Alstine came on the phone and explained that the problem was of basically the same nature as has been suggested for your Hafler amp - bad solder joints on some of the connections between the driver transistors and the board. Repeated thermal stress could eventually cause the joint to become intermittent or open. It was apparently due to the soldering process used... AVA changed the process once they learned of the problem with this batch of amps. He recommended that I reflow the individual solder joints and add a bit of good-quality new solder to each. I did, and it fixed the problem completely. -- Dave Platt AE6EO Hosting the Jade Warrior home page: http://www.radagast.org/jade-warrior I do _not_ wish to receive unsolicited commercial email, and I will boycott any company which has the gall to send me such ads! |
#95
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HELP! Hafler DH-200 misbehaving!
In article ,
Colin B. wrote: Good point. I'm tempted to reflow the board as it is, just because. When we saw the one bad power lead on the board, we did touch up all of the connecting wires (none of them looked very good, actually) but not on the board itself. Speaking of which, it's a phenolic board on this amp. I don't have the serial number right now, but I'll get it when I go home. I'll look closely, but I don't think there are any washers between the transistors and the board, anywhere. I had (have) a Van Alstine Omega 150 amp which developed some odd symptoms - a sharp POP in one channel, anywhere from 15 seconds to a couple of minutes after it was powered on. This occurred intermittently for a couple of years, and then the channel suddenly became extremely noisy (hiss). I phoned AVA, and Frank Van Alstine came on the phone and explained that the problem was of basically the same nature as has been suggested for your Hafler amp - bad solder joints on some of the connections between the driver transistors and the board. Repeated thermal stress could eventually cause the joint to become intermittent or open. It was apparently due to the soldering process used... AVA changed the process once they learned of the problem with this batch of amps. He recommended that I reflow the individual solder joints and add a bit of good-quality new solder to each. I did, and it fixed the problem completely. -- Dave Platt AE6EO Hosting the Jade Warrior home page: http://www.radagast.org/jade-warrior I do _not_ wish to receive unsolicited commercial email, and I will boycott any company which has the gall to send me such ads! |
#96
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HELP! Hafler DH-200 misbehaving!
In article ,
Colin B. wrote: Good point. I'm tempted to reflow the board as it is, just because. When we saw the one bad power lead on the board, we did touch up all of the connecting wires (none of them looked very good, actually) but not on the board itself. Speaking of which, it's a phenolic board on this amp. I don't have the serial number right now, but I'll get it when I go home. I'll look closely, but I don't think there are any washers between the transistors and the board, anywhere. I had (have) a Van Alstine Omega 150 amp which developed some odd symptoms - a sharp POP in one channel, anywhere from 15 seconds to a couple of minutes after it was powered on. This occurred intermittently for a couple of years, and then the channel suddenly became extremely noisy (hiss). I phoned AVA, and Frank Van Alstine came on the phone and explained that the problem was of basically the same nature as has been suggested for your Hafler amp - bad solder joints on some of the connections between the driver transistors and the board. Repeated thermal stress could eventually cause the joint to become intermittent or open. It was apparently due to the soldering process used... AVA changed the process once they learned of the problem with this batch of amps. He recommended that I reflow the individual solder joints and add a bit of good-quality new solder to each. I did, and it fixed the problem completely. -- Dave Platt AE6EO Hosting the Jade Warrior home page: http://www.radagast.org/jade-warrior I do _not_ wish to receive unsolicited commercial email, and I will boycott any company which has the gall to send me such ads! |
#97
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HELP! Hafler DH-200 misbehaving!
In article ,
Colin B. wrote: Good point. I'm tempted to reflow the board as it is, just because. When we saw the one bad power lead on the board, we did touch up all of the connecting wires (none of them looked very good, actually) but not on the board itself. Speaking of which, it's a phenolic board on this amp. I don't have the serial number right now, but I'll get it when I go home. I'll look closely, but I don't think there are any washers between the transistors and the board, anywhere. I had (have) a Van Alstine Omega 150 amp which developed some odd symptoms - a sharp POP in one channel, anywhere from 15 seconds to a couple of minutes after it was powered on. This occurred intermittently for a couple of years, and then the channel suddenly became extremely noisy (hiss). I phoned AVA, and Frank Van Alstine came on the phone and explained that the problem was of basically the same nature as has been suggested for your Hafler amp - bad solder joints on some of the connections between the driver transistors and the board. Repeated thermal stress could eventually cause the joint to become intermittent or open. It was apparently due to the soldering process used... AVA changed the process once they learned of the problem with this batch of amps. He recommended that I reflow the individual solder joints and add a bit of good-quality new solder to each. I did, and it fixed the problem completely. -- Dave Platt AE6EO Hosting the Jade Warrior home page: http://www.radagast.org/jade-warrior I do _not_ wish to receive unsolicited commercial email, and I will boycott any company which has the gall to send me such ads! |
#98
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HELP! Hafler DH-200 misbehaving!
Bugger! I had a nice long post, and most of it got eaten.
Oh well. Here's the weekend's update on the amp. First of all, in answer to Dick's question, it's an early amp, with the phenolic board and S/N 3113059. Now the long and short of my work is that I pulled Q9 and measured it on the bench. It kept coming and going, so I splurged on the $0.30, and put a new one in. Then I went over the thing with a voltmeter, and measured everything on the board. If there was an odd-looking component, I pulled it out and measured it on the bench. If there was an ugly solder joint, I touched it up. Then I went over pretty much all of the traces on the board, paying special attention to the driver transistor leads. Measured the power supply incidentally, and it's sitting at +/-58VDC, on both channels. So far so good. There were some bad solder joints, but everything seems to be working properly. Not much to do but turn it on and see if it works. (as an aside, I am currently lacking both variac and oscilloscope, and won't get them back for a few weeks at least). The results were fairly promising, but first--a diversion! I hadn't noticed before, but Q5 and Q6 have been replaced before. I'm wondering if they're not particularly well balanced, as Dick suggested. Furthermore, I had pulled Q9 and replaced it with an identical...2N5550. Today I noticed on the schematic, that it's supposed to be an NP2222! Checked the other channel, and it too had a 5550 in the bias loop. Both channels' transistors were original, so there was a change at some point between the circuit being made, and the schematic being written up. Now as I said, I turned on the amp to measure any DC offset at the outputs. Everything seemed fine, so I then set the bias back to 220mA, same as I've got on the other channel, and let it run for a while, about 10 minutes. Everything still measured fine after that, but the heat sink and output transistors were decidedly warmer on this channel than the other one. That was enough for me--the amp got turned OFF again. So we have about 30mVDC more on this channel than the other one, and hotter heat sinks for the same bias voltage. The first could be explained by a (fairly small) imbalance between Q5/Q6, but how much heat would that generate? Any guesses folks? I'll probably pull the pair out and measure the hFe, and if they're out of whack, get a matched pair. (The local store has the 2N5550 in bags of 5/$1.49, so I'm hoping to get the 2N5401 similarly packaged, and measure them closely to find a pair). So what next? Thanks, Colin |
#99
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HELP! Hafler DH-200 misbehaving!
Bugger! I had a nice long post, and most of it got eaten.
Oh well. Here's the weekend's update on the amp. First of all, in answer to Dick's question, it's an early amp, with the phenolic board and S/N 3113059. Now the long and short of my work is that I pulled Q9 and measured it on the bench. It kept coming and going, so I splurged on the $0.30, and put a new one in. Then I went over the thing with a voltmeter, and measured everything on the board. If there was an odd-looking component, I pulled it out and measured it on the bench. If there was an ugly solder joint, I touched it up. Then I went over pretty much all of the traces on the board, paying special attention to the driver transistor leads. Measured the power supply incidentally, and it's sitting at +/-58VDC, on both channels. So far so good. There were some bad solder joints, but everything seems to be working properly. Not much to do but turn it on and see if it works. (as an aside, I am currently lacking both variac and oscilloscope, and won't get them back for a few weeks at least). The results were fairly promising, but first--a diversion! I hadn't noticed before, but Q5 and Q6 have been replaced before. I'm wondering if they're not particularly well balanced, as Dick suggested. Furthermore, I had pulled Q9 and replaced it with an identical...2N5550. Today I noticed on the schematic, that it's supposed to be an NP2222! Checked the other channel, and it too had a 5550 in the bias loop. Both channels' transistors were original, so there was a change at some point between the circuit being made, and the schematic being written up. Now as I said, I turned on the amp to measure any DC offset at the outputs. Everything seemed fine, so I then set the bias back to 220mA, same as I've got on the other channel, and let it run for a while, about 10 minutes. Everything still measured fine after that, but the heat sink and output transistors were decidedly warmer on this channel than the other one. That was enough for me--the amp got turned OFF again. So we have about 30mVDC more on this channel than the other one, and hotter heat sinks for the same bias voltage. The first could be explained by a (fairly small) imbalance between Q5/Q6, but how much heat would that generate? Any guesses folks? I'll probably pull the pair out and measure the hFe, and if they're out of whack, get a matched pair. (The local store has the 2N5550 in bags of 5/$1.49, so I'm hoping to get the 2N5401 similarly packaged, and measure them closely to find a pair). So what next? Thanks, Colin |
#100
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HELP! Hafler DH-200 misbehaving!
Bugger! I had a nice long post, and most of it got eaten.
Oh well. Here's the weekend's update on the amp. First of all, in answer to Dick's question, it's an early amp, with the phenolic board and S/N 3113059. Now the long and short of my work is that I pulled Q9 and measured it on the bench. It kept coming and going, so I splurged on the $0.30, and put a new one in. Then I went over the thing with a voltmeter, and measured everything on the board. If there was an odd-looking component, I pulled it out and measured it on the bench. If there was an ugly solder joint, I touched it up. Then I went over pretty much all of the traces on the board, paying special attention to the driver transistor leads. Measured the power supply incidentally, and it's sitting at +/-58VDC, on both channels. So far so good. There were some bad solder joints, but everything seems to be working properly. Not much to do but turn it on and see if it works. (as an aside, I am currently lacking both variac and oscilloscope, and won't get them back for a few weeks at least). The results were fairly promising, but first--a diversion! I hadn't noticed before, but Q5 and Q6 have been replaced before. I'm wondering if they're not particularly well balanced, as Dick suggested. Furthermore, I had pulled Q9 and replaced it with an identical...2N5550. Today I noticed on the schematic, that it's supposed to be an NP2222! Checked the other channel, and it too had a 5550 in the bias loop. Both channels' transistors were original, so there was a change at some point between the circuit being made, and the schematic being written up. Now as I said, I turned on the amp to measure any DC offset at the outputs. Everything seemed fine, so I then set the bias back to 220mA, same as I've got on the other channel, and let it run for a while, about 10 minutes. Everything still measured fine after that, but the heat sink and output transistors were decidedly warmer on this channel than the other one. That was enough for me--the amp got turned OFF again. So we have about 30mVDC more on this channel than the other one, and hotter heat sinks for the same bias voltage. The first could be explained by a (fairly small) imbalance between Q5/Q6, but how much heat would that generate? Any guesses folks? I'll probably pull the pair out and measure the hFe, and if they're out of whack, get a matched pair. (The local store has the 2N5550 in bags of 5/$1.49, so I'm hoping to get the 2N5401 similarly packaged, and measure them closely to find a pair). So what next? Thanks, Colin |
#101
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HELP! Hafler DH-200 misbehaving!
Bugger! I had a nice long post, and most of it got eaten.
Oh well. Here's the weekend's update on the amp. First of all, in answer to Dick's question, it's an early amp, with the phenolic board and S/N 3113059. Now the long and short of my work is that I pulled Q9 and measured it on the bench. It kept coming and going, so I splurged on the $0.30, and put a new one in. Then I went over the thing with a voltmeter, and measured everything on the board. If there was an odd-looking component, I pulled it out and measured it on the bench. If there was an ugly solder joint, I touched it up. Then I went over pretty much all of the traces on the board, paying special attention to the driver transistor leads. Measured the power supply incidentally, and it's sitting at +/-58VDC, on both channels. So far so good. There were some bad solder joints, but everything seems to be working properly. Not much to do but turn it on and see if it works. (as an aside, I am currently lacking both variac and oscilloscope, and won't get them back for a few weeks at least). The results were fairly promising, but first--a diversion! I hadn't noticed before, but Q5 and Q6 have been replaced before. I'm wondering if they're not particularly well balanced, as Dick suggested. Furthermore, I had pulled Q9 and replaced it with an identical...2N5550. Today I noticed on the schematic, that it's supposed to be an NP2222! Checked the other channel, and it too had a 5550 in the bias loop. Both channels' transistors were original, so there was a change at some point between the circuit being made, and the schematic being written up. Now as I said, I turned on the amp to measure any DC offset at the outputs. Everything seemed fine, so I then set the bias back to 220mA, same as I've got on the other channel, and let it run for a while, about 10 minutes. Everything still measured fine after that, but the heat sink and output transistors were decidedly warmer on this channel than the other one. That was enough for me--the amp got turned OFF again. So we have about 30mVDC more on this channel than the other one, and hotter heat sinks for the same bias voltage. The first could be explained by a (fairly small) imbalance between Q5/Q6, but how much heat would that generate? Any guesses folks? I'll probably pull the pair out and measure the hFe, and if they're out of whack, get a matched pair. (The local store has the 2N5550 in bags of 5/$1.49, so I'm hoping to get the 2N5401 similarly packaged, and measure them closely to find a pair). So what next? Thanks, Colin |
#102
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HELP! Hafler DH-200 misbehaving!
If the bias measured the same for both channels, then I would look again for
a DC offset. This assumes a load was connected. You might start by adjusting the bias with NO load. There could be a problem on the load side at this point. Mark Z. -- Please reply only to Group. I regret this is necessary. Viruses and spam have rendered my regular e-mail address useless. "Colin B." wrote in message ... Bugger! I had a nice long post, and most of it got eaten. Oh well. Here's the weekend's update on the amp. First of all, in answer to Dick's question, it's an early amp, with the phenolic board and S/N 3113059. Now the long and short of my work is that I pulled Q9 and measured it on the bench. It kept coming and going, so I splurged on the $0.30, and put a new one in. Then I went over the thing with a voltmeter, and measured everything on the board. If there was an odd-looking component, I pulled it out and measured it on the bench. If there was an ugly solder joint, I touched it up. Then I went over pretty much all of the traces on the board, paying special attention to the driver transistor leads. Measured the power supply incidentally, and it's sitting at +/-58VDC, on both channels. So far so good. There were some bad solder joints, but everything seems to be working properly. Not much to do but turn it on and see if it works. (as an aside, I am currently lacking both variac and oscilloscope, and won't get them back for a few weeks at least). The results were fairly promising, but first--a diversion! I hadn't noticed before, but Q5 and Q6 have been replaced before. I'm wondering if they're not particularly well balanced, as Dick suggested. Furthermore, I had pulled Q9 and replaced it with an identical...2N5550. Today I noticed on the schematic, that it's supposed to be an NP2222! Checked the other channel, and it too had a 5550 in the bias loop. Both channels' transistors were original, so there was a change at some point between the circuit being made, and the schematic being written up. Now as I said, I turned on the amp to measure any DC offset at the outputs. Everything seemed fine, so I then set the bias back to 220mA, same as I've got on the other channel, and let it run for a while, about 10 minutes. Everything still measured fine after that, but the heat sink and output transistors were decidedly warmer on this channel than the other one. That was enough for me--the amp got turned OFF again. So we have about 30mVDC more on this channel than the other one, and hotter heat sinks for the same bias voltage. The first could be explained by a (fairly small) imbalance between Q5/Q6, but how much heat would that generate? Any guesses folks? I'll probably pull the pair out and measure the hFe, and if they're out of whack, get a matched pair. (The local store has the 2N5550 in bags of 5/$1.49, so I'm hoping to get the 2N5401 similarly packaged, and measure them closely to find a pair). So what next? Thanks, Colin |
#103
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HELP! Hafler DH-200 misbehaving!
If the bias measured the same for both channels, then I would look again for
a DC offset. This assumes a load was connected. You might start by adjusting the bias with NO load. There could be a problem on the load side at this point. Mark Z. -- Please reply only to Group. I regret this is necessary. Viruses and spam have rendered my regular e-mail address useless. "Colin B." wrote in message ... Bugger! I had a nice long post, and most of it got eaten. Oh well. Here's the weekend's update on the amp. First of all, in answer to Dick's question, it's an early amp, with the phenolic board and S/N 3113059. Now the long and short of my work is that I pulled Q9 and measured it on the bench. It kept coming and going, so I splurged on the $0.30, and put a new one in. Then I went over the thing with a voltmeter, and measured everything on the board. If there was an odd-looking component, I pulled it out and measured it on the bench. If there was an ugly solder joint, I touched it up. Then I went over pretty much all of the traces on the board, paying special attention to the driver transistor leads. Measured the power supply incidentally, and it's sitting at +/-58VDC, on both channels. So far so good. There were some bad solder joints, but everything seems to be working properly. Not much to do but turn it on and see if it works. (as an aside, I am currently lacking both variac and oscilloscope, and won't get them back for a few weeks at least). The results were fairly promising, but first--a diversion! I hadn't noticed before, but Q5 and Q6 have been replaced before. I'm wondering if they're not particularly well balanced, as Dick suggested. Furthermore, I had pulled Q9 and replaced it with an identical...2N5550. Today I noticed on the schematic, that it's supposed to be an NP2222! Checked the other channel, and it too had a 5550 in the bias loop. Both channels' transistors were original, so there was a change at some point between the circuit being made, and the schematic being written up. Now as I said, I turned on the amp to measure any DC offset at the outputs. Everything seemed fine, so I then set the bias back to 220mA, same as I've got on the other channel, and let it run for a while, about 10 minutes. Everything still measured fine after that, but the heat sink and output transistors were decidedly warmer on this channel than the other one. That was enough for me--the amp got turned OFF again. So we have about 30mVDC more on this channel than the other one, and hotter heat sinks for the same bias voltage. The first could be explained by a (fairly small) imbalance between Q5/Q6, but how much heat would that generate? Any guesses folks? I'll probably pull the pair out and measure the hFe, and if they're out of whack, get a matched pair. (The local store has the 2N5550 in bags of 5/$1.49, so I'm hoping to get the 2N5401 similarly packaged, and measure them closely to find a pair). So what next? Thanks, Colin |
#104
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HELP! Hafler DH-200 misbehaving!
If the bias measured the same for both channels, then I would look again for
a DC offset. This assumes a load was connected. You might start by adjusting the bias with NO load. There could be a problem on the load side at this point. Mark Z. -- Please reply only to Group. I regret this is necessary. Viruses and spam have rendered my regular e-mail address useless. "Colin B." wrote in message ... Bugger! I had a nice long post, and most of it got eaten. Oh well. Here's the weekend's update on the amp. First of all, in answer to Dick's question, it's an early amp, with the phenolic board and S/N 3113059. Now the long and short of my work is that I pulled Q9 and measured it on the bench. It kept coming and going, so I splurged on the $0.30, and put a new one in. Then I went over the thing with a voltmeter, and measured everything on the board. If there was an odd-looking component, I pulled it out and measured it on the bench. If there was an ugly solder joint, I touched it up. Then I went over pretty much all of the traces on the board, paying special attention to the driver transistor leads. Measured the power supply incidentally, and it's sitting at +/-58VDC, on both channels. So far so good. There were some bad solder joints, but everything seems to be working properly. Not much to do but turn it on and see if it works. (as an aside, I am currently lacking both variac and oscilloscope, and won't get them back for a few weeks at least). The results were fairly promising, but first--a diversion! I hadn't noticed before, but Q5 and Q6 have been replaced before. I'm wondering if they're not particularly well balanced, as Dick suggested. Furthermore, I had pulled Q9 and replaced it with an identical...2N5550. Today I noticed on the schematic, that it's supposed to be an NP2222! Checked the other channel, and it too had a 5550 in the bias loop. Both channels' transistors were original, so there was a change at some point between the circuit being made, and the schematic being written up. Now as I said, I turned on the amp to measure any DC offset at the outputs. Everything seemed fine, so I then set the bias back to 220mA, same as I've got on the other channel, and let it run for a while, about 10 minutes. Everything still measured fine after that, but the heat sink and output transistors were decidedly warmer on this channel than the other one. That was enough for me--the amp got turned OFF again. So we have about 30mVDC more on this channel than the other one, and hotter heat sinks for the same bias voltage. The first could be explained by a (fairly small) imbalance between Q5/Q6, but how much heat would that generate? Any guesses folks? I'll probably pull the pair out and measure the hFe, and if they're out of whack, get a matched pair. (The local store has the 2N5550 in bags of 5/$1.49, so I'm hoping to get the 2N5401 similarly packaged, and measure them closely to find a pair). So what next? Thanks, Colin |
#105
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HELP! Hafler DH-200 misbehaving!
If the bias measured the same for both channels, then I would look again for
a DC offset. This assumes a load was connected. You might start by adjusting the bias with NO load. There could be a problem on the load side at this point. Mark Z. -- Please reply only to Group. I regret this is necessary. Viruses and spam have rendered my regular e-mail address useless. "Colin B." wrote in message ... Bugger! I had a nice long post, and most of it got eaten. Oh well. Here's the weekend's update on the amp. First of all, in answer to Dick's question, it's an early amp, with the phenolic board and S/N 3113059. Now the long and short of my work is that I pulled Q9 and measured it on the bench. It kept coming and going, so I splurged on the $0.30, and put a new one in. Then I went over the thing with a voltmeter, and measured everything on the board. If there was an odd-looking component, I pulled it out and measured it on the bench. If there was an ugly solder joint, I touched it up. Then I went over pretty much all of the traces on the board, paying special attention to the driver transistor leads. Measured the power supply incidentally, and it's sitting at +/-58VDC, on both channels. So far so good. There were some bad solder joints, but everything seems to be working properly. Not much to do but turn it on and see if it works. (as an aside, I am currently lacking both variac and oscilloscope, and won't get them back for a few weeks at least). The results were fairly promising, but first--a diversion! I hadn't noticed before, but Q5 and Q6 have been replaced before. I'm wondering if they're not particularly well balanced, as Dick suggested. Furthermore, I had pulled Q9 and replaced it with an identical...2N5550. Today I noticed on the schematic, that it's supposed to be an NP2222! Checked the other channel, and it too had a 5550 in the bias loop. Both channels' transistors were original, so there was a change at some point between the circuit being made, and the schematic being written up. Now as I said, I turned on the amp to measure any DC offset at the outputs. Everything seemed fine, so I then set the bias back to 220mA, same as I've got on the other channel, and let it run for a while, about 10 minutes. Everything still measured fine after that, but the heat sink and output transistors were decidedly warmer on this channel than the other one. That was enough for me--the amp got turned OFF again. So we have about 30mVDC more on this channel than the other one, and hotter heat sinks for the same bias voltage. The first could be explained by a (fairly small) imbalance between Q5/Q6, but how much heat would that generate? Any guesses folks? I'll probably pull the pair out and measure the hFe, and if they're out of whack, get a matched pair. (The local store has the 2N5550 in bags of 5/$1.49, so I'm hoping to get the 2N5401 similarly packaged, and measure them closely to find a pair). So what next? Thanks, Colin |
#106
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HELP! Hafler DH-200 misbehaving!
Pardon me for top posting but I want this material to be "up front" so others
might see it, especially the part about a mod to fix DC offset in these amps. Your soldering skills are excellent and it seems you are zeroing in on success. Did you state you still have a DC offset of 30 mV? Did you "load" that channel with a ~10 ohm 10 watt resistor and then measure for DC offset at the positive speaker terminal referenced to circuit ground? Don't be confused by the NP2222 or PN2222 labels. They are a poor choice in labeling and create confusion. Most any NPN transistor with an hfe of 100 or more should be OK at that part of the circuit. Your sr.# shows your Hafler kit was readied for shipment during the 13th week of 1981 and was a kit, not factory assembled. At this point I would suggest swapping the MOSFETs from one channel to another. It has been my experience that some of the older MOSFETs become "leaky" which could influence bias settings and cause extra heat. I've had some of the P-channel devices that no longer matched the original Hafler grade number and had gone down to a grade level of 1. Also, when checked for leakage they turned out to be too far out of spec to be usable. I have an original Hafler MOSFET checker/grader meter here and it has been helpful. Let us know if the MOSFET swaps from one channel to the other make a difference in bias current and DC offset and heat sink temps. Now, here is the "magic answer" to fixing DC offsets of around 200 mV or less: A CIRCUIT MOD TO FIX DC OFFSET ------------------------------------------------------- This DH-200 DC nulling circuit was described by Walt Jung in The Audio Amateur 1/83, page 56. It is simple and uses a small variable resistor that mounts nicely on the circuit card by drilling 3 small holes with a wire gauge drill (like for drilling holes in a PCB). I drilled my 3 small holes in a vertical line beginning just above where R8 is attached to the + PS rail. The bottom leg of the pot was solder tacked to the + PS rail, the other leg (top pin) is attached to the - PS rail by a short length of insulated wire. The middle pin (wiper) is attached to the junction of R4 and R5 via a 2 megohm 1/4 watt metal film resistor. Just attach a 100Kohm pot between the two power supply rails and feed the output of its wiper through a 2 megohm resistor to where R4 and R5 touch the input trace. I used a miniature 1/2 Watt multi-turn cermet variable resistor. A small value film cap across the legs of the pot would be a good idea to help cancel any noise riding on the PS rails. This little circuit solves a bunch of problems and I don't know why more people don't use it. It is not a destructive mod, just a simple add-on. The pot allows inserting through the 2 meg ohm resistor a very small "sample" of either + or - voltage to the amp's input to null DC offset. I've seen more than one schematic for other amps that routinely do the same thing. Hope this helps. Spread the word! Dick ============================== "Colin B." wrote: Bugger! I had a nice long post, and most of it got eaten. Oh well. Here's the weekend's update on the amp. First of all, in answer to Dick's question, it's an early amp, with the phenolic board and S/N 3113059. Now the long and short of my work is that I pulled Q9 and measured it on the bench. It kept coming and going, so I splurged on the $0.30, and put a new one in. Then I went over the thing with a voltmeter, and measured everything on the board. If there was an odd-looking component, I pulled it out and measured it on the bench. If there was an ugly solder joint, I touched it up. Then I went over pretty much all of the traces on the board, paying special attention to the driver transistor leads. Measured the power supply incidentally, and it's sitting at +/-58VDC, on both channels. So far so good. There were some bad solder joints, but everything seems to be working properly. Not much to do but turn it on and see if it works. (as an aside, I am currently lacking both variac and oscilloscope, and won't get them back for a few weeks at least). The results were fairly promising, but first--a diversion! I hadn't noticed before, but Q5 and Q6 have been replaced before. I'm wondering if they're not particularly well balanced, as Dick suggested. Furthermore, I had pulled Q9 and replaced it with an identical...2N5550. Today I noticed on the schematic, that it's supposed to be an NP2222! Checked the other channel, and it too had a 5550 in the bias loop. Both channels' transistors were original, so there was a change at some point between the circuit being made, and the schematic being written up. Now as I said, I turned on the amp to measure any DC offset at the outputs. Everything seemed fine, so I then set the bias back to 220mA, same as I've got on the other channel, and let it run for a while, about 10 minutes. Everything still measured fine after that, but the heat sink and output transistors were decidedly warmer on this channel than the other one. That was enough for me--the amp got turned OFF again. So we have about 30mVDC more on this channel than the other one, and hotter heat sinks for the same bias voltage. The first could be explained by a (fairly small) imbalance between Q5/Q6, but how much heat would that generate? Any guesses folks? I'll probably pull the pair out and measure the hFe, and if they're out of whack, get a matched pair. (The local store has the 2N5550 in bags of 5/$1.49, so I'm hoping to get the 2N5401 similarly packaged, and measure them closely to find a pair). So what next? Thanks, Colin |
#107
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HELP! Hafler DH-200 misbehaving!
Pardon me for top posting but I want this material to be "up front" so others
might see it, especially the part about a mod to fix DC offset in these amps. Your soldering skills are excellent and it seems you are zeroing in on success. Did you state you still have a DC offset of 30 mV? Did you "load" that channel with a ~10 ohm 10 watt resistor and then measure for DC offset at the positive speaker terminal referenced to circuit ground? Don't be confused by the NP2222 or PN2222 labels. They are a poor choice in labeling and create confusion. Most any NPN transistor with an hfe of 100 or more should be OK at that part of the circuit. Your sr.# shows your Hafler kit was readied for shipment during the 13th week of 1981 and was a kit, not factory assembled. At this point I would suggest swapping the MOSFETs from one channel to another. It has been my experience that some of the older MOSFETs become "leaky" which could influence bias settings and cause extra heat. I've had some of the P-channel devices that no longer matched the original Hafler grade number and had gone down to a grade level of 1. Also, when checked for leakage they turned out to be too far out of spec to be usable. I have an original Hafler MOSFET checker/grader meter here and it has been helpful. Let us know if the MOSFET swaps from one channel to the other make a difference in bias current and DC offset and heat sink temps. Now, here is the "magic answer" to fixing DC offsets of around 200 mV or less: A CIRCUIT MOD TO FIX DC OFFSET ------------------------------------------------------- This DH-200 DC nulling circuit was described by Walt Jung in The Audio Amateur 1/83, page 56. It is simple and uses a small variable resistor that mounts nicely on the circuit card by drilling 3 small holes with a wire gauge drill (like for drilling holes in a PCB). I drilled my 3 small holes in a vertical line beginning just above where R8 is attached to the + PS rail. The bottom leg of the pot was solder tacked to the + PS rail, the other leg (top pin) is attached to the - PS rail by a short length of insulated wire. The middle pin (wiper) is attached to the junction of R4 and R5 via a 2 megohm 1/4 watt metal film resistor. Just attach a 100Kohm pot between the two power supply rails and feed the output of its wiper through a 2 megohm resistor to where R4 and R5 touch the input trace. I used a miniature 1/2 Watt multi-turn cermet variable resistor. A small value film cap across the legs of the pot would be a good idea to help cancel any noise riding on the PS rails. This little circuit solves a bunch of problems and I don't know why more people don't use it. It is not a destructive mod, just a simple add-on. The pot allows inserting through the 2 meg ohm resistor a very small "sample" of either + or - voltage to the amp's input to null DC offset. I've seen more than one schematic for other amps that routinely do the same thing. Hope this helps. Spread the word! Dick ============================== "Colin B." wrote: Bugger! I had a nice long post, and most of it got eaten. Oh well. Here's the weekend's update on the amp. First of all, in answer to Dick's question, it's an early amp, with the phenolic board and S/N 3113059. Now the long and short of my work is that I pulled Q9 and measured it on the bench. It kept coming and going, so I splurged on the $0.30, and put a new one in. Then I went over the thing with a voltmeter, and measured everything on the board. If there was an odd-looking component, I pulled it out and measured it on the bench. If there was an ugly solder joint, I touched it up. Then I went over pretty much all of the traces on the board, paying special attention to the driver transistor leads. Measured the power supply incidentally, and it's sitting at +/-58VDC, on both channels. So far so good. There were some bad solder joints, but everything seems to be working properly. Not much to do but turn it on and see if it works. (as an aside, I am currently lacking both variac and oscilloscope, and won't get them back for a few weeks at least). The results were fairly promising, but first--a diversion! I hadn't noticed before, but Q5 and Q6 have been replaced before. I'm wondering if they're not particularly well balanced, as Dick suggested. Furthermore, I had pulled Q9 and replaced it with an identical...2N5550. Today I noticed on the schematic, that it's supposed to be an NP2222! Checked the other channel, and it too had a 5550 in the bias loop. Both channels' transistors were original, so there was a change at some point between the circuit being made, and the schematic being written up. Now as I said, I turned on the amp to measure any DC offset at the outputs. Everything seemed fine, so I then set the bias back to 220mA, same as I've got on the other channel, and let it run for a while, about 10 minutes. Everything still measured fine after that, but the heat sink and output transistors were decidedly warmer on this channel than the other one. That was enough for me--the amp got turned OFF again. So we have about 30mVDC more on this channel than the other one, and hotter heat sinks for the same bias voltage. The first could be explained by a (fairly small) imbalance between Q5/Q6, but how much heat would that generate? Any guesses folks? I'll probably pull the pair out and measure the hFe, and if they're out of whack, get a matched pair. (The local store has the 2N5550 in bags of 5/$1.49, so I'm hoping to get the 2N5401 similarly packaged, and measure them closely to find a pair). So what next? Thanks, Colin |
#108
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HELP! Hafler DH-200 misbehaving!
Pardon me for top posting but I want this material to be "up front" so others
might see it, especially the part about a mod to fix DC offset in these amps. Your soldering skills are excellent and it seems you are zeroing in on success. Did you state you still have a DC offset of 30 mV? Did you "load" that channel with a ~10 ohm 10 watt resistor and then measure for DC offset at the positive speaker terminal referenced to circuit ground? Don't be confused by the NP2222 or PN2222 labels. They are a poor choice in labeling and create confusion. Most any NPN transistor with an hfe of 100 or more should be OK at that part of the circuit. Your sr.# shows your Hafler kit was readied for shipment during the 13th week of 1981 and was a kit, not factory assembled. At this point I would suggest swapping the MOSFETs from one channel to another. It has been my experience that some of the older MOSFETs become "leaky" which could influence bias settings and cause extra heat. I've had some of the P-channel devices that no longer matched the original Hafler grade number and had gone down to a grade level of 1. Also, when checked for leakage they turned out to be too far out of spec to be usable. I have an original Hafler MOSFET checker/grader meter here and it has been helpful. Let us know if the MOSFET swaps from one channel to the other make a difference in bias current and DC offset and heat sink temps. Now, here is the "magic answer" to fixing DC offsets of around 200 mV or less: A CIRCUIT MOD TO FIX DC OFFSET ------------------------------------------------------- This DH-200 DC nulling circuit was described by Walt Jung in The Audio Amateur 1/83, page 56. It is simple and uses a small variable resistor that mounts nicely on the circuit card by drilling 3 small holes with a wire gauge drill (like for drilling holes in a PCB). I drilled my 3 small holes in a vertical line beginning just above where R8 is attached to the + PS rail. The bottom leg of the pot was solder tacked to the + PS rail, the other leg (top pin) is attached to the - PS rail by a short length of insulated wire. The middle pin (wiper) is attached to the junction of R4 and R5 via a 2 megohm 1/4 watt metal film resistor. Just attach a 100Kohm pot between the two power supply rails and feed the output of its wiper through a 2 megohm resistor to where R4 and R5 touch the input trace. I used a miniature 1/2 Watt multi-turn cermet variable resistor. A small value film cap across the legs of the pot would be a good idea to help cancel any noise riding on the PS rails. This little circuit solves a bunch of problems and I don't know why more people don't use it. It is not a destructive mod, just a simple add-on. The pot allows inserting through the 2 meg ohm resistor a very small "sample" of either + or - voltage to the amp's input to null DC offset. I've seen more than one schematic for other amps that routinely do the same thing. Hope this helps. Spread the word! Dick ============================== "Colin B." wrote: Bugger! I had a nice long post, and most of it got eaten. Oh well. Here's the weekend's update on the amp. First of all, in answer to Dick's question, it's an early amp, with the phenolic board and S/N 3113059. Now the long and short of my work is that I pulled Q9 and measured it on the bench. It kept coming and going, so I splurged on the $0.30, and put a new one in. Then I went over the thing with a voltmeter, and measured everything on the board. If there was an odd-looking component, I pulled it out and measured it on the bench. If there was an ugly solder joint, I touched it up. Then I went over pretty much all of the traces on the board, paying special attention to the driver transistor leads. Measured the power supply incidentally, and it's sitting at +/-58VDC, on both channels. So far so good. There were some bad solder joints, but everything seems to be working properly. Not much to do but turn it on and see if it works. (as an aside, I am currently lacking both variac and oscilloscope, and won't get them back for a few weeks at least). The results were fairly promising, but first--a diversion! I hadn't noticed before, but Q5 and Q6 have been replaced before. I'm wondering if they're not particularly well balanced, as Dick suggested. Furthermore, I had pulled Q9 and replaced it with an identical...2N5550. Today I noticed on the schematic, that it's supposed to be an NP2222! Checked the other channel, and it too had a 5550 in the bias loop. Both channels' transistors were original, so there was a change at some point between the circuit being made, and the schematic being written up. Now as I said, I turned on the amp to measure any DC offset at the outputs. Everything seemed fine, so I then set the bias back to 220mA, same as I've got on the other channel, and let it run for a while, about 10 minutes. Everything still measured fine after that, but the heat sink and output transistors were decidedly warmer on this channel than the other one. That was enough for me--the amp got turned OFF again. So we have about 30mVDC more on this channel than the other one, and hotter heat sinks for the same bias voltage. The first could be explained by a (fairly small) imbalance between Q5/Q6, but how much heat would that generate? Any guesses folks? I'll probably pull the pair out and measure the hFe, and if they're out of whack, get a matched pair. (The local store has the 2N5550 in bags of 5/$1.49, so I'm hoping to get the 2N5401 similarly packaged, and measure them closely to find a pair). So what next? Thanks, Colin |
#109
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HELP! Hafler DH-200 misbehaving!
Pardon me for top posting but I want this material to be "up front" so others
might see it, especially the part about a mod to fix DC offset in these amps. Your soldering skills are excellent and it seems you are zeroing in on success. Did you state you still have a DC offset of 30 mV? Did you "load" that channel with a ~10 ohm 10 watt resistor and then measure for DC offset at the positive speaker terminal referenced to circuit ground? Don't be confused by the NP2222 or PN2222 labels. They are a poor choice in labeling and create confusion. Most any NPN transistor with an hfe of 100 or more should be OK at that part of the circuit. Your sr.# shows your Hafler kit was readied for shipment during the 13th week of 1981 and was a kit, not factory assembled. At this point I would suggest swapping the MOSFETs from one channel to another. It has been my experience that some of the older MOSFETs become "leaky" which could influence bias settings and cause extra heat. I've had some of the P-channel devices that no longer matched the original Hafler grade number and had gone down to a grade level of 1. Also, when checked for leakage they turned out to be too far out of spec to be usable. I have an original Hafler MOSFET checker/grader meter here and it has been helpful. Let us know if the MOSFET swaps from one channel to the other make a difference in bias current and DC offset and heat sink temps. Now, here is the "magic answer" to fixing DC offsets of around 200 mV or less: A CIRCUIT MOD TO FIX DC OFFSET ------------------------------------------------------- This DH-200 DC nulling circuit was described by Walt Jung in The Audio Amateur 1/83, page 56. It is simple and uses a small variable resistor that mounts nicely on the circuit card by drilling 3 small holes with a wire gauge drill (like for drilling holes in a PCB). I drilled my 3 small holes in a vertical line beginning just above where R8 is attached to the + PS rail. The bottom leg of the pot was solder tacked to the + PS rail, the other leg (top pin) is attached to the - PS rail by a short length of insulated wire. The middle pin (wiper) is attached to the junction of R4 and R5 via a 2 megohm 1/4 watt metal film resistor. Just attach a 100Kohm pot between the two power supply rails and feed the output of its wiper through a 2 megohm resistor to where R4 and R5 touch the input trace. I used a miniature 1/2 Watt multi-turn cermet variable resistor. A small value film cap across the legs of the pot would be a good idea to help cancel any noise riding on the PS rails. This little circuit solves a bunch of problems and I don't know why more people don't use it. It is not a destructive mod, just a simple add-on. The pot allows inserting through the 2 meg ohm resistor a very small "sample" of either + or - voltage to the amp's input to null DC offset. I've seen more than one schematic for other amps that routinely do the same thing. Hope this helps. Spread the word! Dick ============================== "Colin B." wrote: Bugger! I had a nice long post, and most of it got eaten. Oh well. Here's the weekend's update on the amp. First of all, in answer to Dick's question, it's an early amp, with the phenolic board and S/N 3113059. Now the long and short of my work is that I pulled Q9 and measured it on the bench. It kept coming and going, so I splurged on the $0.30, and put a new one in. Then I went over the thing with a voltmeter, and measured everything on the board. If there was an odd-looking component, I pulled it out and measured it on the bench. If there was an ugly solder joint, I touched it up. Then I went over pretty much all of the traces on the board, paying special attention to the driver transistor leads. Measured the power supply incidentally, and it's sitting at +/-58VDC, on both channels. So far so good. There were some bad solder joints, but everything seems to be working properly. Not much to do but turn it on and see if it works. (as an aside, I am currently lacking both variac and oscilloscope, and won't get them back for a few weeks at least). The results were fairly promising, but first--a diversion! I hadn't noticed before, but Q5 and Q6 have been replaced before. I'm wondering if they're not particularly well balanced, as Dick suggested. Furthermore, I had pulled Q9 and replaced it with an identical...2N5550. Today I noticed on the schematic, that it's supposed to be an NP2222! Checked the other channel, and it too had a 5550 in the bias loop. Both channels' transistors were original, so there was a change at some point between the circuit being made, and the schematic being written up. Now as I said, I turned on the amp to measure any DC offset at the outputs. Everything seemed fine, so I then set the bias back to 220mA, same as I've got on the other channel, and let it run for a while, about 10 minutes. Everything still measured fine after that, but the heat sink and output transistors were decidedly warmer on this channel than the other one. That was enough for me--the amp got turned OFF again. So we have about 30mVDC more on this channel than the other one, and hotter heat sinks for the same bias voltage. The first could be explained by a (fairly small) imbalance between Q5/Q6, but how much heat would that generate? Any guesses folks? I'll probably pull the pair out and measure the hFe, and if they're out of whack, get a matched pair. (The local store has the 2N5550 in bags of 5/$1.49, so I'm hoping to get the 2N5401 similarly packaged, and measure them closely to find a pair). So what next? Thanks, Colin |
#111
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HELP! Hafler DH-200 misbehaving!
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#112
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HELP! Hafler DH-200 misbehaving!
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#113
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HELP! Hafler DH-200 misbehaving!
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#115
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HELP! Hafler DH-200 misbehaving!
Colin,
SUCCESS! Experience has taught me a good troubleshooting strategy for these amps and the first 4 transistors are almost always the main culprits when too much DC offset is present. And, as you found, the solution is relatively simple for those who have good soldering skills. Dick ========================= "Colin B." wrote: lid wrote: Pardon me for top posting but I want this material to be "up front" so others might see it, especially the part about a mod to fix DC offset in these amps. No problem for me. Your soldering skills are excellent and it seems you are zeroing in on success. Did you state you still have a DC offset of 30 mV? Did you "load" that channel with a ~10 ohm 10 watt resistor and then measure for DC offset at the positive speaker terminal referenced to circuit ground? Don't be confused by the NP2222 or PN2222 labels. They are a poor choice in labeling and create confusion. Most any NPN transistor with an hfe of 100 or more should be OK at that part of the circuit. First of all, I've been doing much of my 'rough 'n' ready' measurements with no load. When I get closer, I toss in an ancient speaker of suspicious origins, but a nominal resistance of 8ohm. As for Q9 not being a NP2222, I didn't think that it would be an issue, but it was rather interesting (not to mention startling, when I first noticed the discrepancy! :-). Your sr.# shows your Hafler kit was readied for shipment during the 13th week of 1981 and was a kit, not factory assembled. Thanks much! Very cool to know. Now we're all on the same page about there being an undesirable DC offset happening, and the real trick is finding it. You had mentioned the Q1/Q2 and Q5/Q6 differential amp pairs, and so I went after them. Q1 and Q2 were matched almost perfectly, (gain of 78 I think), but Q5 and Q6 were quite different: hFe was 70 and 115 respectively, which is a LONG way from 10%! Well, I swapped them with a matched pair and the no-load offset at the speaker terminal went from 55mV down to 7mV. Seven! Everything looks good on the bench, so next step is to plug it into the stereo and let it sit for a while before buttoning it up. At this point I would suggest swapping the MOSFETs from one channel to another. It has been my experience that some of the older MOSFETs become "leaky" which could influence bias settings and cause extra heat. I've had some of the P-channel devices that no longer matched the original Hafler grade number and had gone down to a grade level of 1. Also, when checked for leakage they turned out to be too far out of spec to be usable. I have an original Hafler MOSFET checker/grader meter here and it has been helpful. Let us know if the MOSFET swaps from one channel to the other make a difference in bias current and DC offset and heat sink temps. I'm hoping that this isn't necessary. It looks like it won't be, so I've got my fingers crossed. Now, here is the "magic answer" to fixing DC offsets of around 200 mV or less: A CIRCUIT MOD TO FIX DC OFFSET This is sooo simple that I'll probably do it as soon as I've got all of my other projects bottled up and out of the way. Brilliant solution to the problem here! So we may (fingers crossed) have a working and stable amp--and in better shape than when I got it. I'll keep you posted. Colin |
#116
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HELP! Hafler DH-200 misbehaving!
Colin,
SUCCESS! Experience has taught me a good troubleshooting strategy for these amps and the first 4 transistors are almost always the main culprits when too much DC offset is present. And, as you found, the solution is relatively simple for those who have good soldering skills. Dick ========================= "Colin B." wrote: lid wrote: Pardon me for top posting but I want this material to be "up front" so others might see it, especially the part about a mod to fix DC offset in these amps. No problem for me. Your soldering skills are excellent and it seems you are zeroing in on success. Did you state you still have a DC offset of 30 mV? Did you "load" that channel with a ~10 ohm 10 watt resistor and then measure for DC offset at the positive speaker terminal referenced to circuit ground? Don't be confused by the NP2222 or PN2222 labels. They are a poor choice in labeling and create confusion. Most any NPN transistor with an hfe of 100 or more should be OK at that part of the circuit. First of all, I've been doing much of my 'rough 'n' ready' measurements with no load. When I get closer, I toss in an ancient speaker of suspicious origins, but a nominal resistance of 8ohm. As for Q9 not being a NP2222, I didn't think that it would be an issue, but it was rather interesting (not to mention startling, when I first noticed the discrepancy! :-). Your sr.# shows your Hafler kit was readied for shipment during the 13th week of 1981 and was a kit, not factory assembled. Thanks much! Very cool to know. Now we're all on the same page about there being an undesirable DC offset happening, and the real trick is finding it. You had mentioned the Q1/Q2 and Q5/Q6 differential amp pairs, and so I went after them. Q1 and Q2 were matched almost perfectly, (gain of 78 I think), but Q5 and Q6 were quite different: hFe was 70 and 115 respectively, which is a LONG way from 10%! Well, I swapped them with a matched pair and the no-load offset at the speaker terminal went from 55mV down to 7mV. Seven! Everything looks good on the bench, so next step is to plug it into the stereo and let it sit for a while before buttoning it up. At this point I would suggest swapping the MOSFETs from one channel to another. It has been my experience that some of the older MOSFETs become "leaky" which could influence bias settings and cause extra heat. I've had some of the P-channel devices that no longer matched the original Hafler grade number and had gone down to a grade level of 1. Also, when checked for leakage they turned out to be too far out of spec to be usable. I have an original Hafler MOSFET checker/grader meter here and it has been helpful. Let us know if the MOSFET swaps from one channel to the other make a difference in bias current and DC offset and heat sink temps. I'm hoping that this isn't necessary. It looks like it won't be, so I've got my fingers crossed. Now, here is the "magic answer" to fixing DC offsets of around 200 mV or less: A CIRCUIT MOD TO FIX DC OFFSET This is sooo simple that I'll probably do it as soon as I've got all of my other projects bottled up and out of the way. Brilliant solution to the problem here! So we may (fingers crossed) have a working and stable amp--and in better shape than when I got it. I'll keep you posted. Colin |
#117
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HELP! Hafler DH-200 misbehaving!
Colin,
SUCCESS! Experience has taught me a good troubleshooting strategy for these amps and the first 4 transistors are almost always the main culprits when too much DC offset is present. And, as you found, the solution is relatively simple for those who have good soldering skills. Dick ========================= "Colin B." wrote: lid wrote: Pardon me for top posting but I want this material to be "up front" so others might see it, especially the part about a mod to fix DC offset in these amps. No problem for me. Your soldering skills are excellent and it seems you are zeroing in on success. Did you state you still have a DC offset of 30 mV? Did you "load" that channel with a ~10 ohm 10 watt resistor and then measure for DC offset at the positive speaker terminal referenced to circuit ground? Don't be confused by the NP2222 or PN2222 labels. They are a poor choice in labeling and create confusion. Most any NPN transistor with an hfe of 100 or more should be OK at that part of the circuit. First of all, I've been doing much of my 'rough 'n' ready' measurements with no load. When I get closer, I toss in an ancient speaker of suspicious origins, but a nominal resistance of 8ohm. As for Q9 not being a NP2222, I didn't think that it would be an issue, but it was rather interesting (not to mention startling, when I first noticed the discrepancy! :-). Your sr.# shows your Hafler kit was readied for shipment during the 13th week of 1981 and was a kit, not factory assembled. Thanks much! Very cool to know. Now we're all on the same page about there being an undesirable DC offset happening, and the real trick is finding it. You had mentioned the Q1/Q2 and Q5/Q6 differential amp pairs, and so I went after them. Q1 and Q2 were matched almost perfectly, (gain of 78 I think), but Q5 and Q6 were quite different: hFe was 70 and 115 respectively, which is a LONG way from 10%! Well, I swapped them with a matched pair and the no-load offset at the speaker terminal went from 55mV down to 7mV. Seven! Everything looks good on the bench, so next step is to plug it into the stereo and let it sit for a while before buttoning it up. At this point I would suggest swapping the MOSFETs from one channel to another. It has been my experience that some of the older MOSFETs become "leaky" which could influence bias settings and cause extra heat. I've had some of the P-channel devices that no longer matched the original Hafler grade number and had gone down to a grade level of 1. Also, when checked for leakage they turned out to be too far out of spec to be usable. I have an original Hafler MOSFET checker/grader meter here and it has been helpful. Let us know if the MOSFET swaps from one channel to the other make a difference in bias current and DC offset and heat sink temps. I'm hoping that this isn't necessary. It looks like it won't be, so I've got my fingers crossed. Now, here is the "magic answer" to fixing DC offsets of around 200 mV or less: A CIRCUIT MOD TO FIX DC OFFSET This is sooo simple that I'll probably do it as soon as I've got all of my other projects bottled up and out of the way. Brilliant solution to the problem here! So we may (fingers crossed) have a working and stable amp--and in better shape than when I got it. I'll keep you posted. Colin |
#118
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HELP! Hafler DH-200 misbehaving!
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#119
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HELP! Hafler DH-200 misbehaving!
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